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顺煤层钻孔聚氨酯长距离快速封孔测压技术
供稿: 杨宏民;王启宇 时间: 2018-11-19 次数:

作者:杨宏民王启宇

作者单位:河南省瓦斯地质与瓦斯防治重点实验室(省部共建国家重点实验室培育基地)河南理工大学安全科学与工程学院

摘要:顺煤层长钻孔采用聚氨酯封孔必须解决聚氨酯初始发泡时间、注入方式、封堵方式等关键工艺问题。通过在南庄12号煤层的现场试验,采用35 m封孔段长度、1∶1.25的聚氨酯黑白料配比、两堵一注封孔方式,测得煤层瓦斯压力为0.39~0.74 MPa,成功解决了顺煤层钻孔测不出煤层瓦斯压力的问题,其最大测值比瓦斯压力反演值低19.57%,说明聚氨酯封孔本煤层测压仍存在技术难度大、测值偏低等问题,但研究结果对于同类条件下瓦斯压力的准确测定具有指导意义。

基金:国家自然科学基金资助项目(51174081);河南省重大科技攻关项目(092102310037);

关键词:顺煤层钻孔;聚氨酯;封孔;快速测定技术;

DOI:10.16186/j.cnki.1673-9787.2015.01.002

分类号:TD712

Abstract:When using polyurethane for gas pressure measurement in an along-coal-seam hole,the first foaming time of polyurethane,the methods of injection and sealing are the key technologies that must be solved.In the site test of No.12 coalbed in Nanzhuang coal mine,the results indicated that when sealing length is more than35 m,the polyurethane ratio between black and white materials is 1∶1.25,and when using the method of injecting polyurethane into and between two blocks,the problem of measuring the pressure is resolved successfully,and the maximum measuring gas pressure is 19.57 percent smaller than the inversion calculation value.The research indicates that the alone-coal-seam hole-sealing using polyurethane is still the technical problems of more difficulty and smaller measured-value,but the results of the study still have a certain instructional significance to similar engineering applications.

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